1. Introduction
2. Numerical Wave Tank
2.1 Numerical Analysis Method
2.2 Verification of the Numerical Wave Tank (NWT)
3. Optimal Cross-Section Analysis
3.1 Optimal Cross-Section of Low Crest Deign
3.2 Optimal Cross-Section of Slit Deign
3.3 Optimal Cross-Section of Upper-Level Drainage Channel Design
3.4 Optimal Cross-Section of Lower-Level Drainage Channel Deign
4. Conclusions
The overall hydraulic characteristics were reproduced effectively. This is based on the fact that the differences between experimental and calculated values for KR, KT, and KD were less than ±10%. The agreement between these in terms of the water level behind the structure was approximately 90%. This verifies the effectiveness and validity of the NWT used.
With regard to the first factor in enhancing the efficiency of the submerged breakwater, an increase in crest width (B) and a decrease in crest depth (R) were effective for wave control. Owing to the wave-breaking effect caused by the ratio of the crest depth to the incident wave height (R / Hi), the water level behind the structure increased as the crest depth (R) decreased. However, it tended to decrease gradually again under the influence of the slit and drainage channels.
Second, an increase in slit width (BS) was highly effective in reducing the water level behind the structure. As the slit distance (DS) decreased, it effectively reduced the water level behind the structure. However, the wave control efficiency was similar or marginally lower.
Third, an increase in upper-level drainage channel size (SU) tended to improve wave control and the efficiency of reducing the water level behind the structure. Meanwhile, the impact of the upper-level drainage channel height (hU) on these was insignificant.
Fourth, an increase in lower-level drainage channel size (SL) was effective in reducing the water level behind the structure. However, it had no significant impact on the wave control effects.
The optimal cross-section of the submerged breakwater was determined to be for a case in which SU ≥ 1.8Hi. In this case, the water level behind the structure decreased by over 72%, and wave control improved by over 10%.







